360 cu in (5.9 L) Magnum V8 - 230 hp/325 lb.ft. 4-speed A518(46RH)
Torqueflite Automatic Transmission Dana 60's Front & Rear, 3.54F/3.55R
1.5" Rear Lift & 2.5" Front Leveling Kit 37x12.50r17 B.F. Goodrich
All-Terrain T/A's Mile Marker 12,000# Winch
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Here is the truck as I picked it up from the farm. It has 345,xxx
miles on it and starts up every time you hit the key. There is some
noise in the front end, the tires are shoot, there is also an exhaust noise
and some rust and body damage. The AC is not currently working but had
worked great in the past, likely a freon leak. The AC controls is
missing a couple of knobs as well. The seats and floor covering as
well as the headliner are toast. The brake lights quite working, but
the turn signals and 3rd brake light work.
Pulled out the floor covering and old seats and shoveled the dirt out of the
floor before installing a good set of seats, all though they are tan rather
than gray.
Picked up a set of new 17" steel wheels to mount the 37" BFG's I had on
hand. They fit the truck nicely with a little fender clearance issue
at the rear of the front fenders when turning.
To address the front end noise, steering issues and tire clearances I
proceeded to install a 2.5" leveling kit as well as a set of RUKSE
Heavy Duty Adjustable Control Arms. These control arms will allow me to move the axle
forward to maintain the proper wheelbase/suspension component alignment with
the leveling kit as we as give be the fender clearance. I also
replaced the shocks and upper and lower ball joints as well as sway bar
links and bushings.
I've installed new brake pads, pistons and calipers as well as a complete
brake system flush. I've also replaced a leaking rear axle seal and
started the body repairs. The interior trim panels are all removed and
cleaned and I'm awaiting some new fabric for the headliners and working
speakers.
Installed a new cover on the headliner and a new carpet. I also
cleaned all the interior trim panels and re-installed them along with
new/additional speakers and an aftermarket radio.
I recycled and repaired the Mile Marker 12K that was my Trailer Recovery
Winch and installed it. Still a few finishing details, and it won't be
completely installed until I pull the bumper for painting and add a weld or
two on where I had to widen and extend the frame rails. Next comes the
sanding, filling, sanding, repeat and finally paint.
Since David had removed the old plastic bed protector that had been in the
truck since it was new, I found the rust was a little worse than expected in
some areas, and not as bad as was feared in others. So I cleaned and rust
protected the Bed as well as lining it with Bed Liner (Raptor by U-Pol). I
did sand the tailgate down to metal and re-prime it with Epoxy Primer.
2016-11-06
After diagnosing and gutting the old electronics from the Mile Marker Winch
control, leaving only the solenoids, I connected a Harbor Freight wireless
controller to make it operable. I also found I had broke one of the terminal
leads for the field in the motor and had to remove it and have it fixed. I
was then able to finish connect and test the winch, and all works well. I
also had to replace the Power Steering pump, as the one I'd installed
earlier had started leaking. While I was at it it also got all new hoses.
Changed the oil and filter now that it had 4K miles since the last change.
2016-11-07
The 4WD CAD is now operatable from inside the Cab. I added a manual
vacuum valve to the inside of the cab to operate it. Now I can have
both 2WD and 4WD low range, oh and not have to crawl under the truck to
engage/disengauge the axle. You can also see the power switch to
supply power to the front mounted winch. With the help of some heat
and a candle I was finally able to remove the old (now throwing codes) O2
Sensor and replace it. 2016-11-08
I found that the sway bar link at ride height and front end compression was
hitting the coil spring axle pocket. Now with the Sway bar drop kit
installed thought that it was fixed, but it showed the real problem. I
thought at first it was just the Moog Link Grease Zerk hitting the steering
link, but even replacing it with a smaller zerk, that was not going to
prevent the link and tie rod from hitting on compression and/or turns. So
the solution? Remove the drop brackets I'd installed and return the sway bar
back to it's stock location and flip the sway bar links to rotate the sway
bar up and move the links away from any suspension/steering items. Now no
more interference and they clear the tires/springs etc... 2016-11-11